All my deliveries turned up today and so this job has rapidly (I hope) come to completion. I decided to recoil the front five head studs and leave the long ones at the back alone.
Apart from taking things apart and making sure all is clean, the first thing to do was to drill the over-sized holes for the recoil kit. The kit came with the required drill which was a nice touch. It also came with the thread insertion tool, and a tang break-off tool and of course, the tap.
Now, these holes have to be absolutely in the right place (because even though the actual cylinder head has over-sized clearance holes, the head gasket does not). As well, the holes have to be square with the top surface of the block, otherwise one might end up with a crooked head stud which would be most unfortunate. The only good way to do this with the block in the car is with a magnetic drill. The first picture below shows the setup.
Although the holes pass through into the water jacket, we only need to drill to the thread depth and so it is best to put a felt pen mark on the drill to indicate this, otherwise we might go too deep and hit something else down there.
Once the hole has been drilled, the drill is removed and the tap inserted into the drill chuck. This is to make sure that the tap is square and in the same place as the drill. Turing the chuck about one turn by hand will get the tap started, then the chuck can be loosened and the drill removed, and the rest of the thread cut with a tap wrench.
Dilling and tapping in cast iron is usually pretty easy as long as with the drill, the speed is kept down. If you cut cast iron too quickly, it heats up and becomes hard, and you find you'll have great diffiulty in making any progress. The magnetic drill I used had a rotational speed of about 350 rpm which worked very well.
Once the tap has done its work, the recoil insert is wound in with the tool, and then the tang at the bottom broken off with the magnetic push rod supplied. However, the magnetic push rod wasn't strong enough to actually grab hold of the tang and so all of them fell into the water jacket. That was OK because other than masking up all the cylinder bores and push rod holes, I had to fish out all the swarf with a stick magnet anyway.
I gave the new head studs (which, by the way looked far better finished than the old ones) a short spray with hylomar on the bottom threads (since they go into the water jacket and need to be sealed) and screwed them in just past finger tight.
The moment of truth came when I put the head gasket on. It wouldn't go on at first, which caused me some moments of panic, but then I realised it was just catching on one of the long studs and a little push, and down it went.
The head went on, along with all the other bits and pieces, and I am glad to say in torqued up just fine to the regulation 40 ft lb. I started filling up with water when I realised I'd forgotton about the bypass hose. Luckily the night before I'd put a small amount of rubber grease on it and when the head went on the hose slipped over the spigot and all I had to do was to tighten the clamp.
I did use the special washers I made up with the centering boss and they clipped in very nicely. So now I know the studs are all centred in the holes. Whether or not they'll sink in like the old standards ones did I don't know yet, but so far so good.
I'd like to thank the kind people at MinisPlus in Melbourne to sent me the new cylinder head studs and went to the trouble of making personal contact to discuss the job.
So, I'll leave things overnight and check tension again tomorrow before starting up. I suppose I'll spend the rest of the evening looking for those two rocker cover tube nuts that I must have put in a safe place but now cannot be found.
regards, Tony
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