Ausmini
It is currently Sun Aug 17, 2025 1:49 pm

All times are UTC + 10 hours




Post new topic Reply to topic  [ 8 posts ] 
Author Message
 Post subject: She Works Man!
PostPosted: Fri Sep 23, 2005 11:14 pm 
Offline
1275cc
1275cc
User avatar

Joined: Sat Aug 07, 2004 8:41 am
Posts: 2047
Location: Grays Point
Well it appears we now have my car working properly (save for a but of a tune with the gas analyser when I have the time!)!!!!

Guess what it was.

On the back of the HIF44 (well at least on the one I have anyway), there are 3 small holes which need air flow through them. I think two of them have something to do with the piston moving up and down, and the third is a breather for the float bowl.

Anyways remember how I said no matter how rich a needle we put in there it was just ending up lean, well apparantly the carby doesn't like it at all when you block that float bowl breather hole off!!! :shock:

Now I know what you're all thinking - Bob f^&ked it up. :roll:
Well there's a little story behind that too. :?
I bought a K&N filter, but the only one they make that fits with the GR manifold is the offset one for the 1 1/2" SU, so you have to ream the holes out to suit. Hours of fun with a die grinder.

Now, I didn't know which of the holes needed air flow, so I did the logical thing and opened it up for all of them. Not neat, but does the job. Didn't have a gasket so used silastic.

All good. You all saw it like that at the Dyno day, and apart from the fueling problems (that was the choke O-ring gone - more of a C-ring!!) it went ok. I got 2nd in class at the khanacross the following day so something must work.

Went back to Grahams to try and sort it out, and everyone's fabourite K1w1 (Jai) graciously put a kit through the carb for me.

Remember how I said I didn't have a gasket? Well there was one in the kit, so naturally Jai used it to replace my bodgy silastic job. No more problems with fuel bleeding through from the choke - but now car ran too lean!! Stuffed around with it there for a few hours (I've nearly had a contract taken out on me by the missus because of the time/money I've spent on this car!!) and no matter what needle we used we just couldn't get it to run right. Had today off and put the Weber back on to make sure it was the carby that was the problem. Not neck snapping performance, but ran nicely. Jets WAY to small for monster engine now, but it still went OK and proved that it was my carb that was the issue.

Apparently Graham doesn't like something as simple as an SU beating him so he started to investigate. Blew some compressed air through a couple of holes. It was a classic. He was just saying something like there's gotta be a blockage here somewhere when he blew some air up the fuel pickup and we heard the tell tale psssssh.....POP noise.

That new gasket didn't have a hole in the right spot!!!! ARRRRGH!!! :twisted:
Oh well at least it was a simple fix in the end!!

Tried another needle in it and it goes fine. When time permits we'll get the gas analyser onto it and tune it all up properly, but for now it goes quite well - especially since the throttle linkage I have is a piece of crap and I'm only getting about 70% throttle when my foot's to the floor!!!

All I need now is a decent exhaust, some 1.5 rockers and full throttle and it should go like crap off a shovel!!!

[/epic post]

_________________
Bob Slattery
Duffman Says A Lot of Things - OH YEAH!!


Top
 Profile  
 
 Post subject:
PostPosted: Fri Sep 23, 2005 11:27 pm 
Offline
ET 13.457 seconds , OH YEAH !!!!
User avatar

Joined: Sun Sep 19, 2004 8:35 am
Posts: 7826
Location: Somewhere Around Sydney
Congrats Bob, i'm sure it was worth it in the end 8)

_________________
Image
Starlet Conversion:
http://www.ausmini.com/forums/viewtopic.php?t=15484


Top
 Profile  
 
 Post subject:
PostPosted: Fri Sep 23, 2005 11:38 pm 
Offline
the King of Bling
User avatar

Joined: Thu Jun 03, 2004 11:11 pm
Posts: 19858
Location: Baulkham Hills
Bob Thats great you have found the problem
NOw she will be flying...you have to love the HIf44 :wink:

Was it the Filter side :?:

_________________
Stop Licking the Dog...I Don't Care Who Started It


Top
 Profile  
 
 Post subject:
PostPosted: Fri Sep 23, 2005 11:51 pm 
Offline
1275cc
1275cc
User avatar

Joined: Sat Aug 07, 2004 8:41 am
Posts: 2047
Location: Grays Point
Yeah, it was where I was saying I had just used silastic to mount my filter housing to the carb - there was a filter housing gasket in the carb kit. Moral of the story - check gaskets first - don't just trust they'll fit out of the box :? :?

_________________
Bob Slattery
Duffman Says A Lot of Things - OH YEAH!!


Top
 Profile  
 
 Post subject:
PostPosted: Sat Sep 24, 2005 6:29 am 
Offline
1275cc
1275cc
User avatar

Joined: Thu May 13, 2004 4:41 pm
Posts: 4418
Location: sydney
Glad to see it is now running as it should. It seemed odd that a rekitted Carb wasn't doing the job. The thing couldn't have been that bad even off a volvo! Well I reckon before you spend anymore money on performance parts i reckon you should tuck those wheels uner some arches, because it is only going to be a metter of time before mr Police man pays you a visit and defects the poor dear. :roll:
Good to see you yesterday, always good for laugh to stir you up :lol:

Cheers

Aaron

_________________
Image


Top
 Profile  
 
 Post subject:
PostPosted: Sat Sep 24, 2005 8:37 am 
Offline
religious status
religious status
User avatar

Joined: Fri Mar 19, 2004 6:19 pm
Posts: 39764
Location: near Baulkham Hills, NSW
Hey Bob,
Good to see you guys yesterday, glad you sussed it out at last.....
Sold the Weber to GR yet?? 8)

_________________
DrMini- 1970 wasaMatic 1360, Mk1S crank, 86.6HP (ATW) =~125 @ crank, 45 Dellorto (38 chokes), RE282 sprint cam, 1.5 rockers, 11.0:1 C/R. :mrgreen:


Top
 Profile  
 
 Post subject:
PostPosted: Sat Sep 24, 2005 4:31 pm 
Offline
998cc
998cc

Joined: Tue Apr 06, 2004 4:30 pm
Posts: 871
Location: welington new zealand
HI Bob glad to hear it got sorted out in the end, i must just point out that i didnt do the back gasket i gave that to you to do and you had a play with aaron (sounds bad) with the solastic stuff(makes it sound even worse) i just did the kit inside and gave it graciously back to you, graham was telling me about the breather hole and i have bought my su manual home to check it out as none other carbs i have played with have had this issue before.
well done and enjoy driving it now and dont kill it.
Now you want to put it on the dyno and see what it does.

_________________
www.minicranks.com add me to your watch list and come back again soon, under construction.


Top
 Profile  
 
 Post subject:
PostPosted: Sat Sep 24, 2005 4:42 pm 
Offline
1275cc
1275cc
User avatar

Joined: Thu May 13, 2004 4:41 pm
Posts: 4418
Location: sydney
I wasn't there when he put the carb back on. I had gone home already as i had already had my fill at laughing at bob getting the raidator out :lol: So it was either Bob or Jye. I know who i am betting on :) God love ya bob!

Cheers

Aaron

_________________
Image


Top
 Profile  
 
Display posts from previous:  Sort by  
Post new topic Reply to topic  [ 8 posts ] 

All times are UTC + 10 hours


Who is online

Users browsing this forum: Bing [Bot] and 389 guests


You cannot post new topics in this forum
You cannot reply to topics in this forum
You cannot edit your posts in this forum
You cannot delete your posts in this forum
You cannot post attachments in this forum

Jump to:  

© 2016 Ausmini. All garage work involves equal measures of enthusiasm, ingenuity and a fair degree of irresponsibility.