G'day all......it was nice to meet you smokie

, sorry i wasn't able to speak to you for very long due to swearing and cursing at my car

on satuday. well the weekend got really bad on sunday

on my "in lap" as i was rounding "the hay shed" heading for lukey heights my engine decided to go "BANG!" at 145km/h @ 5500rpm 4th gear, good oil presure, 60 psi, temp 190 deg F

, as soon as i heard that i shut it down selected neutral and coasted to the marshalling piont between the " hays shed" and "lukey heights" anyways after being towed back to the pits, inspected as much as i could, found it had locked up/seized

(in gear and rock, engine not turning OH F@$K this is gunna be expensive and the "boss" (aka: wife, minister of finance, war, etc......) is not gunna be happy when i tell her this........thank goodness she was only disappointed that i was unable to "race" it anymore and all the prep for it seems to have gone to waste!!) anyways got another few goes

in another team mates mx5 but had to stick to my nominated times, which wasnt had due to the down pour for the last 2ish hours!! That was interesting, could not see a damn thing down the main straight at 180+km/h especially if there was someone anywhere there before you!!

Will be there next year with bells on!!

bigger, better and stronger (depending on what condition the block is in? its possibly going to be

1310, scatter cam, metro a plus head.....etc.....etc...... hopefully ready for "Watto's Grand Day Out"

)

Anyways now its home i have pulled the head off to reveal that No. 2 piston has well and truely hit the head as it has a good imprint of it in the top of the piston...

..so will be pulling the rest of the engine out tommorrow, splitting the block and g/box for what broke

. im hoping for a broken rod at the little end but suspect its a stuffed crank. Will let you know what i find.