Hi Pete, sorry, I've been away for work for the last fortnight.
Well I had it running for 20 minutes or so the morning before I left, but just idling in the garage while I mucked around with the timing. It spat out a little coolant but I know I filled the rad too full, so it would've just been that I'm thinking.
But looking at the two caps and the length of the neck, I can see that even without any pressure, the old cap would have been sitting above the hole for the overflow hose, so I'm pretty sure that will be it.
I can't test drive it just yet as I'm replacing the dizzy with one of ConvertibleMini's you-beaut' electronic units. I just got back today and have a couple of parts to change and timing to reset before I move it anywhere. I probably wont get around to it until later next week...
_________________ '77 Leyland Mini Van
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